Shiftchange
New Member
I have a 1988 Sea Ray 390 EC with 7.4 l mercs. I replace my port motor with a re-manufactured one. I broke it in exactly like the manual said. (20 hr oil change, used the merc oil as spec'd, never went under 1500 rpm's or over 3000 rpm's & kept changing speeds etc) 60 hrs later it failed. My boat neighbor went through the same thing. I was wondering if any one else with the 390 EC has had problems. Is there anything that can eliminate this problem from happening again.
The engine remanufacture company told me that somehow water got into #8 piston chamber & caused a hydraulic lock, which bent the connecting rod. My question: Is there a flap or anything in the exhaust manifold that may need to be replaced to keep this from happening again?? Maybe a blockage??? Any ideas or thoughts???
The engine remanufacture company told me that somehow water got into #8 piston chamber & caused a hydraulic lock, which bent the connecting rod. My question: Is there a flap or anything in the exhaust manifold that may need to be replaced to keep this from happening again?? Maybe a blockage??? Any ideas or thoughts???